My '74 2.0 Restoration introduction... Dyno results!
- falcor
- Posts: 201
- Joined: Mon Aug 27, 2012 7:44 am
Re: My '74 2.0 Restoration introduction...
Started tackling the oil leak today. On inspection I saw that the left valve cover was pushed upwards, probably happened when I pushed the spring in place.
I also took down the starter motor hoping to find a reason for it squealing a bit when the engine starts but I couldnt find anything. I put the starter in my vice and hooked it up to a spare battery and it runs flawlessly.
https://youtu.be/fiwULhbUrrg
Here's a clip of benchtesting the starter.
https://youtu.be/h6CsDYiB2YI
Here's a clip of the engine start efter putting the starter back on the car.
Any ideas on how to fix the annoying squealing noise?
I also took down the starter motor hoping to find a reason for it squealing a bit when the engine starts but I couldnt find anything. I put the starter in my vice and hooked it up to a spare battery and it runs flawlessly.
https://youtu.be/fiwULhbUrrg
Here's a clip of benchtesting the starter.
https://youtu.be/h6CsDYiB2YI
Here's a clip of the engine start efter putting the starter back on the car.
Any ideas on how to fix the annoying squealing noise?
- falcor
- Posts: 201
- Joined: Mon Aug 27, 2012 7:44 am
Re: My '74 2.0 Restoration introduction...
Squealing noise turns out to probably be the throwout bearing.....I'll need to tackle that before tuning I think.
- falcor
- Posts: 201
- Joined: Mon Aug 27, 2012 7:44 am
Re: My '74 2.0 Restoration introduction...
The last few weeks has been spend fixing issues found after getting the engine to start reliably. The biggest hurdle was the throwout bearing. Last weekend the gearbox came out and I ordered a new throwout bearing and all the associated small parts.
While waiting for the parts to arrive i cleaned up the seats. They need to be recovered eventually but for now the California patinated cracked and torn vinyl will have to do. This passenger seat is the better of the two.
I also cadded up some baseplates for the new velocity stacks and had them lasercut at work. A good friend of mine got them welded up tonight.
For my birthday earlier this week I also had a package arrive that I ordered about a month ago. Two custom front mats with the Martini Racing colours.
Pics here: http://www.914world.com/bbs2/index.php? ... 294&st=140
Cant be bothered making a separate size of pictures just for stf.
While waiting for the parts to arrive i cleaned up the seats. They need to be recovered eventually but for now the California patinated cracked and torn vinyl will have to do. This passenger seat is the better of the two.
I also cadded up some baseplates for the new velocity stacks and had them lasercut at work. A good friend of mine got them welded up tonight.
For my birthday earlier this week I also had a package arrive that I ordered about a month ago. Two custom front mats with the Martini Racing colours.
Pics here: http://www.914world.com/bbs2/index.php? ... 294&st=140
Cant be bothered making a separate size of pictures just for stf.
- falcor
- Posts: 201
- Joined: Mon Aug 27, 2012 7:44 am
- aircooledtechguy
- Posts: 1709
- Joined: Sun Oct 28, 2001 1:01 am
Re: My '74 2.0 Restoration introduction...
I'm really happy for you Mats. You've given that car quite a beautiful transformation so far. It looks like you'll have it all wrapped-up by summer and be enjoying it with the top down when the warm weather gets there.falcor wrote:https://www.youtube.com/watch?v=t2cFQvHEeQA
- falcor
- Posts: 201
- Joined: Mon Aug 27, 2012 7:44 am
Re: My '74 2.0 Restoration introduction...
Thanks Nate, apparently someone's upset at my progress tho because right now we have two inches of snow outside and more is falling....
- aircooledtechguy
- Posts: 1709
- Joined: Sun Oct 28, 2001 1:01 am
Re: My '74 2.0 Restoration introduction...
It is that time of year right??
- falcor
- Posts: 201
- Joined: Mon Aug 27, 2012 7:44 am
Re: My '74 2.0 Restoration introduction...
About due for a bit of an update here....
Had the car back together for a booked dyno tuning day on May 9th. Long story short, Engine started puking oil from the passenger side valve cover and making a bad noise around 5000 rpm. I've been happier....
Oil seemed fine but a leakdown test showed 40% leakage on the #3 cylinder. Since I could not find the source of the noise I bit the bullet and shipped out my spare 1.7 Engine to GBOT in Denmark for a 78x96 build.
New engine should be done sometime in august.
Had the car back together for a booked dyno tuning day on May 9th. Long story short, Engine started puking oil from the passenger side valve cover and making a bad noise around 5000 rpm. I've been happier....
Oil seemed fine but a leakdown test showed 40% leakage on the #3 cylinder. Since I could not find the source of the noise I bit the bullet and shipped out my spare 1.7 Engine to GBOT in Denmark for a 78x96 build.
New engine should be done sometime in august.
- falcor
- Posts: 201
- Joined: Mon Aug 27, 2012 7:44 am
Re: My '74 2.0 Restoration introduction...
Well its been awhile since the last update.....but here goes.
https://www.youtube.com/watch?v=QGGdYYHBmTo
Dynoed the new 2256 engine today. (78 stroke 96 bore) Web 86b/c, 10:1 compression, 40 mm itb's and efi.
http://matsgarage.com/wp-content/upload ... -36-51.jpg
https://www.youtube.com/watch?v=QGGdYYHBmTo
Dynoed the new 2256 engine today. (78 stroke 96 bore) Web 86b/c, 10:1 compression, 40 mm itb's and efi.
http://matsgarage.com/wp-content/upload ... -36-51.jpg
- aircooledtechguy
- Posts: 1709
- Joined: Sun Oct 28, 2001 1:01 am
Re: My '74 2.0 Restoration introduction... Dyno results!
That looks like it will be a riot to drive now!! Congrats!!
- falcor
- Posts: 201
- Joined: Mon Aug 27, 2012 7:44 am
Re: My '74 2.0 Restoration introduction... Dyno results!
Thanks Nate!
Apprently the gearbox input shaft seal took offence to having to start to work again and sprung a leak so 48 hours after the dyno I had to take the gearbox out of the car. Waiting for a new seal now.
Apprently the gearbox input shaft seal took offence to having to start to work again and sprung a leak so 48 hours after the dyno I had to take the gearbox out of the car. Waiting for a new seal now.
- aircooledtechguy
- Posts: 1709
- Joined: Sun Oct 28, 2001 1:01 am
Re: My '74 2.0 Restoration introduction... Dyno results!
Old cars,. . . There's always something, huh?
- falcor
- Posts: 201
- Joined: Mon Aug 27, 2012 7:44 am
Re: My '74 2.0 Restoration introduction... Dyno results!
Whoopiiii!
Apparently its now roadlegal.... got the inspection done today and it passed!
Apparently its now roadlegal.... got the inspection done today and it passed!
- falcor
- Posts: 201
- Joined: Mon Aug 27, 2012 7:44 am
- falcor
- Posts: 201
- Joined: Mon Aug 27, 2012 7:44 am