Dyno-time!
Today I took a trip along with Kalle to Hamar around 150km from Oslo for a dyno shoot out
Departure from our hangar around 7 o'clock this morning. The car stood on the dyno a little before 10am and we managed 9 or 10 pulls all togheter.
Some struggling because the boost solenoid fails to compensate pressure on top of the wastegate spring before 50% compensation, so I need to either replace it or clean it inside and check for pulsing.
In addition, I'll re-route the lines to the solenoid and wastegate. Just so the solenoid can get some " cleaner "air to work with.
Engine runs PIG rich! About. 10.2 to 10.5 while it is spooling. That allows the injector duty cycle to hit the ceiling of 100% ... So much for 900cc flow tested injectors.
But .. By leaning out, that can be enough to pull down the DC to maybe around 90%. Maybe...
ID1000 Injector is said to handle 450 engine horses on E85.
Ignition wise we are relatively kind to the engine at 17 degrees at 1.8 bar. Very kind really.
So there is plenty potential left!
The turbo soups some oil, and I've ordered a T3 / T4 rebuild kit.
Today's happy news is 369hk on 5650omdr and 517nm on 4650omdr! And this is at the wheel!