Funky compression results
Posted: Sun Oct 27, 2019 6:07 am
So, for a little background. 2316 build 80mm dpr crank webcam 86a grind, kB 96mm pistons in stock cut cylinders. So. Had motor in car, ran fairly decent. Then one day poof runs like crap got to hot. Got it home, had wifey crank on it and noticed smoke around base of intake on #1 compression results said something was wrong with number one. Took motor down, found compression leak at head, lapped cylinders, rechecked deck height, found the other issue (extra shim, stupidest of stupid mistakes) fixed back together ran compression.
Here’s where the question arises. Compression results are consistent but funky. #1-110 #2-125 #3-110 #4-125. Yes flywheel side is consistently 15lbs weaker than pulley side. Checked valve adjustment, checked cam lift all check good. What else should I check?????? Any insight would be appreciated cause I don’t want to have to pull this motor out of this beetle again. It was running great till the compression thing and I want to get it back to that point!!
Thanks in advance!!
-Brian
Here’s where the question arises. Compression results are consistent but funky. #1-110 #2-125 #3-110 #4-125. Yes flywheel side is consistently 15lbs weaker than pulley side. Checked valve adjustment, checked cam lift all check good. What else should I check?????? Any insight would be appreciated cause I don’t want to have to pull this motor out of this beetle again. It was running great till the compression thing and I want to get it back to that point!!
Thanks in advance!!
-Brian